CrispyEdd
Member
She's been a bit laggy and turbo coming in heavy and ferocious, so suspected sticky VNT or shot turbo.
First run on motorway and she's flying, too good it turned out! Up a hill at 70MPH behind aa= Porsche Boxster 718, I put my foot down shot past and then all turbo power lost - into limp mode?!. GUTTED, a new car - turbo issues - classic rookie purchase I thought, as I let the Porche 718 back past pretending to fiddle with stereo!
Restarting engine gave turbo back again. Quick check on forum....
Checked and traced all the little pipes off the N75 vacuum manifold on offside inner wing (black plastic box with 6 pipes), unclipped the manifold refitted it. All looked good so had that feeling of turbo doom.
Then I found the vacuum pipe from the air intake to the N75 manifold, which is just below and infront (toward front of car) the airflow sensor on the big intake pipe from the air filter, it was about 2mm from being fitted flush, so wiggled it gently back up tight.
To me it looked okay anyway but thought I'd better push it all the way up as its the only thing that I could find that was wrong looking.
Started car and all sorted! Lag reduced by half turbo sucky whistle almost completely gone, earlier smoother power and quieter car. INSANE!!!!
LOVE THIS CAR Hope it helps in future!
First run on motorway and she's flying, too good it turned out! Up a hill at 70MPH behind aa= Porsche Boxster 718, I put my foot down shot past and then all turbo power lost - into limp mode?!. GUTTED, a new car - turbo issues - classic rookie purchase I thought, as I let the Porche 718 back past pretending to fiddle with stereo!
Restarting engine gave turbo back again. Quick check on forum....
Checked and traced all the little pipes off the N75 vacuum manifold on offside inner wing (black plastic box with 6 pipes), unclipped the manifold refitted it. All looked good so had that feeling of turbo doom.
Then I found the vacuum pipe from the air intake to the N75 manifold, which is just below and infront (toward front of car) the airflow sensor on the big intake pipe from the air filter, it was about 2mm from being fitted flush, so wiggled it gently back up tight.
To me it looked okay anyway but thought I'd better push it all the way up as its the only thing that I could find that was wrong looking.
Started car and all sorted! Lag reduced by half turbo sucky whistle almost completely gone, earlier smoother power and quieter car. INSANE!!!!
LOVE THIS CAR Hope it helps in future!